Lil'John
08-10-2009, 03:22 PM
Thought I'd condense my other post down and hopefully get some fresh ideas. This issue is it idles like a champ. But any throttle and it bogs down.
Here is the setup:
2004 LQ4 from Silverado 2500HD swapped into an old Cruiser
NV4500 swapped in place of the stock 4l80e it came with
e8248 fuel pump
Corvette regulator and filter combo(AC Delco P# GF822)
exhaust leak on passenger side
no cats
VATS programmed out as well as rear o2 sensor (JET DTS programmer)
STOCK harness with un-needed junk pulled(autotranny wires, rear o2 wires, and purge valve)... only the VSS wires were removed from the PCM plug and put back on.
headers
new hard and flex lines throughout (3/8" and 6an but also about 12" of 5/16" at tank)
VSS installed
Drive by wire system installed
everything else stock
I've got engine block grounded directly to the battery... all other stock grounds for the harness are at stock locations.
Engine sat for about 8 months before being run.
Things I've done/tested so far:
fuel pressure is at 60psi
soaked injectors in sea foam (no change)
run engine with a can of sea foam and about 7 gal of 87 oct gas (no change)
no engine codes aside from no MIL (P0650)
checked the TB butterfly to ensure it opens both with and without the engine running
replaced a E2000 fuel pump with e8248
confirmed MAF functionality by pulling MAF away from TB as well as unplugging. Both cause the engine to idle like crap.
Would the PCM not having input from the auto tranny spaz it out?
Would a plugged fuel filter cause this? Even though it is still giving the right pressure reading.
Here is the setup:
2004 LQ4 from Silverado 2500HD swapped into an old Cruiser
NV4500 swapped in place of the stock 4l80e it came with
e8248 fuel pump
Corvette regulator and filter combo(AC Delco P# GF822)
exhaust leak on passenger side
no cats
VATS programmed out as well as rear o2 sensor (JET DTS programmer)
STOCK harness with un-needed junk pulled(autotranny wires, rear o2 wires, and purge valve)... only the VSS wires were removed from the PCM plug and put back on.
headers
new hard and flex lines throughout (3/8" and 6an but also about 12" of 5/16" at tank)
VSS installed
Drive by wire system installed
everything else stock
I've got engine block grounded directly to the battery... all other stock grounds for the harness are at stock locations.
Engine sat for about 8 months before being run.
Things I've done/tested so far:
fuel pressure is at 60psi
soaked injectors in sea foam (no change)
run engine with a can of sea foam and about 7 gal of 87 oct gas (no change)
no engine codes aside from no MIL (P0650)
checked the TB butterfly to ensure it opens both with and without the engine running
replaced a E2000 fuel pump with e8248
confirmed MAF functionality by pulling MAF away from TB as well as unplugging. Both cause the engine to idle like crap.
Would the PCM not having input from the auto tranny spaz it out?
Would a plugged fuel filter cause this? Even though it is still giving the right pressure reading.